Sansui AU-9500: Restoration
Normally when starting the restoration process I organize all the parts so that I can quickly replace the faulty ones in the shortest time possible. And this is what I did in this case.
Here is a batch of Panasonic stacked film non polarized capacitors. Very good for stage coupling. They are rated 1 uF / 50 V. As you can see, two of them are already missing because they were just mounted in the equalizer block.
And here are about a hundred KSA992 transistors. I am using them in hFE matched pairs that I discover with my transistor tester. I ordered a lot of them because they are very cheap and having more than necessary is perfect for sorting purposes. Careful with these transistors as their terminals are designated as ECB. The old 2SA726 are BCE. So the replacements must be mounted in reverse.
Next, I scored about a hundred 2SC1845 transistors. I am using them in sorted by hFE pairs as well. Also, care should be taken with these transistors as their terminals are designated as ECB. The old 2SC1313 are BCE. So the replacements must be mounted in reverse. A great but weird particularity of these transistors is that I have measured about 20 of them from the entire lot and all have the same hFE of 428. So no need to sort. I will however test them before soldering.
Sorting transistors, however, is a boring task that requires a lot of patience and time.
This thing is dwarfing my workplace. I had a hard time positioning the unit on my bench.
General Considerations
I should begin by saying that working on this amplifier presents a very big health hazard. There are lethal voltages inside. Not knowing what you are doing might result in severe accidents and possibly death by electrocution. I am very skilled in electronics repair and I have been doing such repairs for almost 20 years. This qualifies me to work in this field. But if you do not have experience, please take this information just as a knowledge base. Do not attempt to repair something that you cannot handle as there is a big probability to severe it further while also suffering accidents.
Good working condition tools are also necessary for this restoration. I am using a quality temperature regulated soldering station with multiple tips for every situation that I could possibly encounter. Also, I am using a good solder pump and quality desoldering wick in two sizes. Isopropyl alcohol is handy to decontaminate boards of old flux and other residues. I also use eutectic formulation quality solder. Every replacement part is brand new, from a reputable manufacturer, ordered from U.S.A., Japan, or Germany. Also, I only use parts that are suitable as replacements in various sections of the amplifier, after inspecting and comprehending the original schematic. Last but not least I have the years of experience backing up every action that I take while working on this unit.
I have found out that working with a temperature of exactly 300 degrees Celsius is sane for these vintage printed circuit boards. I have never lifted a pad with this temperature. But it is also true that I never wait more than three seconds with the soldering tip on a pad. While working on the chassis, I am pumping up between 360 and 440 degrees Celsius in the soldering iron.
Flux fumes are extremely toxic and should be avoided at all costs. Especially toxic are the fumes released while working on these old Japanese electronic boards.
Power Supply / Chassis Restoration
On the chassis there are four really large filtering capacitors. I have tested these against the specifications and they are doing fine. So no replacement for these yet. But I am already searching at my favorite electronic parts store for future-proof replacements. While ordering spare parts I need to be really careful so that they will be identical in diameter and hopefully better than the originals on ripple current filtering. I am still searching and once I will find what I am looking for, I will revisit this page.
However there are some capacitors that I have decided to change. I am talking about C010, C011, C012, C013, rated 4.7 uF / 100 V in the schematic. In my unit they are 3.3 uF / 100 V. I have used Nichicon MUSE KZ series replacements rated 10 uF / 100 V. These capacitors provide local filtering and decoupling of the supply rails for the two driver boards. So bigger is better in this case. I was thinking about bypassing these with 100nF / 100 V non-polarized polypropylene capacitors to cut up on high-frequency oscillations, should they appear. But I have had a hard time observing such oscillations with my 100 MHz oscilloscope. Thus, I quickly abandoned this idea.
Left chanel before.
And after.
Right chanel before.
And after.
It is fairly easy to work on the chassis. But I have used a high power 80 W soldering iron because of the steel chassis. It works like a massive heatsink and the smaller irons will be quickly drained of caloric energy. A large tip helps as well.
F-2030-2 Power Supply / Protector Board Restoration
This board is really easy to remove but you need to note the order of the wires that are attached to it. Besides four soldered wires, all the other wires are using connectors. I have used a 1 mm permanent marker to mark the order of the cables. Before mounting the board back, I will use isopropyl alcohol to wipe clean the cables so that my markings will be erased. The four heavy duty power wires which are soldered are very easy to desolder using a vacuum pump and a powerful iron. I managed to easily desolder them without damaging anything, in about two to three seconds of heat application.
Inspecting the board reveals that there is a number of twelve electrolytic capacitors. I have decided to let alone most of the transistors on this board. Beware that this board has very large ground planes so soldering and desoldering capacitors is difficult to impossible for a low power soldering tool. What I use is a Weller 80 W electronically controlled temperature soldering station with appropriate tips. You do not want to damage tracks of these unobtainium printed circuit boards. So good tools and a lot of precaution is necessary for a clean job.
The board prior to the restoration.
Detailed view on the relay and the coils. In my case the OMRON relay is in very good working order up until one point. And it appears it is the original part. The issue is that from times to times, the relay armature is not assuring a perfect electrical contact and the right channel drops. I have decided to replace the relay with the OMRON MY2-02-DC24 modern counterpart. It is expensive but it worths every cent.
I used Nichicon MUSE KZ series capacitor replacements for the old ELNA ones. These capacitors are fairly large in diameter and also in height. I dare to say that in most cases they are even the same size as the original parts. So I changed the two 220 uF / 75 V capacitors with 220 uF / 100 V capacitors. Then I changed the two 100 uF / 75 V capacitors with 100 uF / 100 V parts. C057 was rated at 470 uF / 16 V. The replacement is 470 uF / 25 V. Regarding the replacements for C060 and C062, I have used the same 220 uF / 50 V rating for both of them. C907 is used as filter for the protector circuit. It was originally rated at 100 uF / 50 V. I replaced it with the same rating modern counterpart. In the protection circuit, C901 and C902 were bipolar capacitors, originally rated at 47 uF / 10 V. I replaced both of them with Nichicon ES series 47 uF / 16 V bipolar parts. C908 is a 1 uF / 50 V bipolar capacitor. I have replaced it with the same type modern part. C906 is part of the relay delay circuit and was originally rated at 1000 uF / 6.3 V. My replacement is a Sprague part rated at 1000 uF / 16 V and 105 ℃.
The board after the job.
The new relay.
And the relay mounted on the printed circuit board.
Then I have proceeded to renewing of all solder joints on the back side of the board. I am using quality eutectic solder.
F-2029 Driver Board Restoration
These two power amplifier sections are the easiest printed circuit boards to work on of them all. There are only four capacitors and two transistors to change per board. There is also a thermal fuse glued on top of a small signal transistor. If you want you can take care of removing that one too. I did as there is no apparent need for a thermal fuse in this part of the circuit. Furthermore some of these amplifiers come from the factory without thermal fuses. I think my unit is part of a newer revision.
Here is the board prior to refurbishing.
The filtering capacitors are designated as C815 and C817. Originally they were rated at 47 uF / 80 V. I have used Nichicon MUSE KZ series rated at 47 uF / 100 V. They fit like a glove. C801 is used as an input capacitor and is rated at 2.2 uF / 50 V. I used a Nichicon FG series capacitor of the same characteristics. C807 is originally rated at 220 uF / 6.3 V. I have replaced it with a Nichicon MUSE KZ series capacitor rated at 220 uF / 25 V.
Transistors TR801 and TR803 are the input differential pair and are of type 2SA726. They are known to develop annoying hiss and crackling sound in time. As a matter of fact, this Sansui amplifier cracks after a few minutes of use. Also, it has a disturbing hiss when idling. I don't want to take any chances and I have decided to replace these transistors as well. I have used hFE matched KSA992 transistors.
As said above, I also took care of the fuse. The glue is very corrosive so I thoroughly removed it with isopropyl alcohol. The fuse is mounted in series with a resistor. I have removed the thermal fuse and soldered the resistor directly in its place, as factory-marked on the board.
And here is the board after the restoration.
Here you can see a detailed view of one of the 47 uF / 100 V replacement capacitors.
On the soldering side I carefully looked for faulty joints. There were none. But I am preparing for the long future so I renewed the solder joints using the eutectic soldering alloy.
The other channel is following as well. This is before restoration.
Detailed view on the thermal fuse. I experimented a bit after dismantling this fuse. So I triggered it with the soldering iron. Once popped there is no means to reset. Or so I think.
And after the job.
Detailed view of the hFE matched KSA992 transistors.
The other channel enjoys the same soldering renewal treatment.
F-2006A Equalizer Board Restoration
Removal of the board is extremely simple. The procedure is to first remove the two side screws holding the steel Faraday cage. The the cage itself. After that you gently pull the board upright out of its socket.
Working on this board is easy as well. There are a twelve capacitors and at least two transistors to change. Why at least? Because there are two 2SA726 transistors which are mandatory to change. But there are another two 2SC1313 transistors. While these are not yet causing issues, as a prevention, you can change these with 2SC1845. I decided to change all of them.
This is the board before restoration.
C601 and C602 are the input stage coupling capacitors. Originally they were 1 uF / 50 V, electrolytic. I have changed them with 1 uF / 50 V Panasonic stacked film capacitors. C603 and C604 which were originally 10 uF / 10 V were replaced with 10 uF / 16 V Nichicon ES series bipolar capacitors. C607 and C608, originally 47 uF / 6.3 V were replaced with 47 uF / 16 V Nichicon ES series bipolar counterparts. C613 and C614 are used to stabilize the static functioning point of two transistors and were originally rated at 47 uF / 6.3 V. I have used 47 uF / 16 V Nichicon FG series replacements. C615 and C616 are part of the RIAA correction network and originally were 4.7 uF / 50 V. I have replaced them with 4.7 uF / 50 V Nichicon ES series bipolar parts. The output coupling stage capacitors, originally rated at 3.3 uF / 50 V were replaced with 3.3 uF / 50 V Nichicon ES series bipolar capacitors.
And after.
On the back side I have renewed the solder joints.
F-2019B Tone Control Board Restoration
Removal of the board is extremely difficult. The procedure involves removing of the power supply board. Then the metallic shielding cage. After you have access to the solder side of the board which is bolted to the chassis with six screws. There is another fixing point in the left side, near the local filtering capacitors. This one requires a powerful soldering iron to detach. But this is not all. There are also a whole lot of wires attached to the solder side of this board. So I decided to let this board alone and adopt a different approach. I have positioned the amplifier so that I can easily reach the components from beneath, while having enough space to work on the solder side. It is an awkward job but the wires were untouched.
This is the board before restoration.
C701 and C702 are the input stage coupling capacitors. They are rated 470 nF / 25 V and are of tantalum type. I really cannot imagine why they have chosen this type of capacitor when it is clear that had the oversized mylar film green drops in production. Better dielectric for audio purposes and less problems caused should these capacitors fail. I have measured these old tantalum ELNA capacitors with my tester. Capacity is ranging from 460 nF (left) to 570 nF (right) while ESR is ranging from 29 R (left) to 120 R (right). Clearly out of specifications. Because I forgot to order replacements for these along with all the other parts, I have sorted through my capacitors box and found two Philips MKT orange drops rated 470 nF / 63 V. They fit like a glove on the PCB. On the tester, ESR is 0.9 R and leakage is 0 for both. Measured capacity is 467 nF. Even though they are not new, I believe they do qualify. Regarding their sound, it is fine. I like it. I have some experience with these capacitors in various tube amplifiers that I have built in the past. No disappointments yet.
The local emitter decoupling capacitors C703, C704, C705, C706, C719, C720 were originally rated 47 uF / 6.3 V. I have used Nichicon MUSE KZ series replacements rated 47 uF / 25 V. Stage coupling capacitors C709, C710, C723, C724, C731, C732 were rated 4.7 uF / 50 V. Nichicon FG series 4.7 uF / 50 V were used as replacement. I have used the same counterparts for C717, C718 2.2 uF / 50 V stage coupling capacitors. The local filtering capacitors C733 and C734 were 220 uF / 35 V. I have used Nichicon MUSE KZ series capacitors rated 220 uF / 50 V. The same for C799, originally 220 uF / 25 V, now replaced with new MUSE KZ series part of the same rating.
There are a also six 2SA726 and six 2SC1313 transistors to change on this board. I have used hFE matched pairs as before. In my unit the first preamplification stage was very noisy. It is constructed around two 2SK30 FET transistors. I have used NOS Toshiba 2SK30Y replacements. There are also two 2SC1364 transistors on this board. I have replaced these with KSC1845 which apparently work very well in this circuit.
Overall this board is very boring to work on. It took me at least four hours to exchange all the parts, due to the difficult clearance and maintenance access. Progress is very slow and barely visible. But I finished it after all. Here it is.
On the back side I have renewed the solder joints.
Beautiful track layout.
In respect to Kosaku Kikuchi and his team that designed this amplifier, I didn't want to have European parts in this amplifier. So I have sourced two Nichicon mylar film capacitors to replace the Philips MKT parts in the input coupling stage.
A little bit bulky but they do fit.
This board concludes the replacement of parts in this audio amplifier.
Miscellaneous
While having this amplifier on my bench I also redid the soldering of various other joints on all the other boards scattered around. I am not going to step into details as there is nothing interesting. But here is a picture.
Also, these packs of RCA connectors were suffering from transportation damage.
The repair was done with spare parts from disassembled units. I got the parts from eBay. An array of RCA jacks came from dismantling of a Sansui AU-101 and another array came from a Sansui 8080DB unit. When dismantled, they look as such.
Wire forest nightmare.
Fabricating the ground planes from pure copper multi-wire cable which I tinned with leaded solder.
Soldering the wires to the new RCA array.
More wires...
Done soldering the wires. The array looks like this.
In the end it looks like this.
RIP RCA array #1.
The other one comes up next. This is before.
From the other side of the array we can see that the board has developed some big transversal cracks. This array is compromised.
Upon dismantling the wires, the array board disintegrated when I wanted to get it out.
RIP RCA array #2.
Now let me show how I slowly rebuilt the RCA bracket. I have salvaged all the components from the old array and resoldered everything in place.
Oh No! More Wires.
All soldered back where they should be.
This is how the RCA array looks now.
Aftermath
Old parts.
This is everything that I did on this amplifier in the electrical field.
Electrical Settings
A final touch of the restoration is performing the electrical settings as illustrated in the service manual. Thus, there are two main settings that I need to touch before putting the case back on.
- Output of Power Amplifier Section
- Current Alignment of Power Amplifier Section
The procedure for setting the output of the power amplifier DC voltage is very simple and clearly detailed in the manual. First, commute the Speakers selector to SYSTEM-A position. Then connect a DC voltmeter to the SYSTEM-A left terminals. Set the scale of the DC voltmeter to 20 mV. Adjust VR801 of the left channel up until the voltmeter reads 0 mV ±10 mV. Repeat this step for the right channel. This time adjust VR801 of the right channel. I have managed to set the DC offset to 0.3 mV. on both channels
Adjusting the idling current of the power amplifier is done by removing the speaker fuses on the back of the unit. First, unscrew the holder for fuse F002. Turn Speakers selector to OFF position. Connect DC ammeter on the terminals of F002 fuse. Adjust VR803 of the left channel for a reading between 30 mA and 40 mA. Repeat the procedure for the right channel. This time remove fuse F003 and adjust trimmer VR803 of the right channel. I have set the bias to 35.0 mA on both channels.
Needless to say that you need to power the unit off each time you remove the fuses. It can be done with the unit powered but there could be a risk to short-circuit terminals and blow off the nice output power transistors.
Electrical Measurements
I decided to test this amplifier against the rated specifications using the signal generator, frequency counter, and oscilloscope. My setup is as follows, given that I conduct the measurements one channel at a time.
- Power on test equipment and let them warm up for half an hour or so.
- Power on audio amplifier and let it warm up for at least 10 minutes.
- Set signal generator output voltage to .775 V.
- Connect signal generator output to amplifier AUX input.
- Connect frequency counter to Speaker output.
- Connect oscilloscope to Speaker output.
- Start the measurements.
Measuring 12 Hz sinewave. In the service manual the rated bandwidth starts at 15 Hz.
Measuring 1 kHz sinewave.
Measuring 40 kHz sinewave. Amplifier output drops considerably but it still amplifies a clean sinewave.
As a bonus, measuring 1 kHz squarewave. Looks funny but then again, my signal generator is not very good with the square wave function.
I tried measuring sinewaves up until 80 kHz. Surprise, the amplifier still does its job. However oscillations start to appear and output drops a lot.
Cleaning the Front Panel
If you ask me, besides the sonic qualities, this is one of the most important things. I cannot stand dirty units. I believe keeping them dirty is equivalent to disrespecting them and the work that was put on them. So I proceeded to disassemble everything on the front panel and clean up all the parts.
Beautiful detail.
The black felt between the up-down switches has been cleaned with isopropyl alcohol and was installed back in its place.
The cleaning of the knobs comes up next. Unfortunately one of them is scratched and I don't have the means to repair it.
Cleaning of the up-down switch caps follows next.
Now it is time to put back the cover of this amplifier and off it goes for another 40 years, in my living room this time.
♫
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